Volume 2
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22
November 2006 |
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Norman
King, QFM Flight Operations Administrator, reported from Southend:
"The report for today is somewhat brief, with the pictures hopefully
saying it all. In a nutshell, the pressurisation test was done with
minimal leakage detected and rectification was done, another 5 minute
job done and dusted. The crew arrived at the aeroplane late in the
afternoon to run through check lists and procedures and we left them
at the controls with the power unit grinding away to provide them
with light. They are coming up to speed rapidly. We have all been
invited to drinks with Ian Dorling and are looking forward to the
evening with one of natures gentlemen." |
23
November 2006 |
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"Ridgeback in the left seat, Feebs in the right seat, Muz in
the observer's seat, H at the panel, Plukka to complete the walk around
after the disconnect then to board up through the Lower 41. Green
Hornet in position at Left 1. Engineers Wilkinson and Finney on board
as observers. Ben Hunter, Bob Horn and I were ready to trail the aeroplane
in a Lasham's truck to scrutinise the exterior, looking for anything
appearing where it wasn't supposed to. We pushed XBA back onto the
taxiway at 1204, ready for engine start, the order being 3, 4, 2,
1. Away went #3, then #4. All routine. Denis Martin on the headset
and Robert Phillips swapped sides to observe the left wing in preparation
for #2's start. As we watched from the ramp we waited for their positions
to change to monitor #1 but they remained in place, in front of #2.
A slight delay, perhaps? Then, the tell tale signs. A plume of atomised
fuel appeared from #2's tailpipe, to clear after about 15 seconds.
A wet start was aborted and the engine motored for 30 seconds to clear
the fuel in the tailpipe. The start lever was lifted again to bring
in the ignitors and in nearly every case, a light off occurs. Damn,
there's no heat haze but instead, another misty exhaust appears and
we are the exception to the rule. #2 wet started three times and the
mission was aborted. How embarrassment. The crew shut down and the
tug brought our pride and joy back onto the ramp. We failed to taxi.
The crowds who had gathered outside Lasham's and the Coffee Shop plane
spotters who had been monitoring 127.725 shrugged their collective
shoulders and slowly dissipated. A longish session of troubleshooting
lay ahead for Peter and the engineering team." |
24
November 2006 |
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"On arrival at SEN, we waited for an answer to Lasham's search
for a Pressurising & Dump Valve, the component diagnosed as the problem
behind the failure to start #2. They found one in the country and
an urgent order was made to send it to ATC Lasham's. No problem, delivery
will be around 1300. Bob Horn and Ben Hunter were assigned the task
of replacing the valve and commenced the removal. It's past 1300 but
no valve. 1430 and no valve. By 1730 and still no valve, we were told
that the precious bit had been dispatched to ATC Lasham's alright,
but to the other branch in Hampshire. First time we have had this
during the 5 months since Peter has been on station. So, with the
crew discovering how the entertainment system works, Plucka polishing
cowls, Green Hornet scrubbing sinks and polishing pots, Roy painting
red rings around dripsticks, Norm Mac finding and repairing leaking
oxygen lines, we were steadily engaged in making the old girl even
tidier. By tomorrow morning, the valve should have arrived, so with
a modicum of luck and a big effort by Bob and Ben, we may be starting
all four around lunch time." |
25
November 2006 |
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"We changed the P&D Valve, the component all the experts pointed
to as the reason for our dilemma. So much for the experts. We changed
the Fuel Control Unit, the next most likely to be the offender. So
much for that one. We ran the dragon so many times for the spins and
start attempts that now the best engine on the aeroplane is unanimously
voted to be the APU's. The hardest working unit on the aeroplane is
the #2 starter motor. The only upside to all this is that we are dripped
on by Jet A1, not Skydrol. Oh, and rain too, as the dynamic SEN W/X
sends some squally winds and showers as we pack up for the night.
We may be a bit physically dampened but don't feel frustrated, disappointed
or disheartened. We have a job to do here and we'll get it done, this
being only a prolonged minor nuisance. There is a reason for the failure
and we will soon find it. On a more people focused note, we will bid
a fond farewell to our youngest volunteer who goes home tomorrow,
Ben Hunter. What an effort Ben has put in, one of two currently employed-by-Qantas
engineers who have taken annual leave to give time to the Project.
Robert Phillips is the other. More about him later. Ben leaves on
tomorrow's QF2 and with him will go a fine brain, cool demeanour and
inspirational work ethic. We'll farewell him at his favourite restaurant
tonight. See ya soon, Ben and thank you so very much for being such
a fine young man." |
26
November 2006 |
|
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"The failures of last night behind us, the plan today is to swap
the engine fuel pump with a brand newy we were carrying as flight
spares. Bob Horn and I, already reeking of kero from yesterday's FCU
change, are the elected ones. We change the pump in Australian and
Commonwealth record time, well inside the time allowed to build the
new Wembley Stadium, and we prepared the engine for a run. New ignitors
add to the odds of a start. The result? The aforementioned starter
motor some say is a misnomer, since it hasn't started anything for
so long, once again swishes into life and the fan starts to rotate.
The rpm is building and eventually the correct revs are achieved and
the start lever goes to Start and once again - fuel vapour and no
light off. On a positive note, the stainless steel manufacturer's
data plate was attached to the aeroplane's primary structure today,
with Denis Martin, Paul Wilkinson, Bob Horn and finally, Peter Elliott
in turn riveting one corner each. We pack it in and head home, after
yet another move to another bay, for that long. hot shower and dinner
to farewell our Flight Control Guru, Roy Finney. As we've mentioned
before, the flight control integrity is largely due to Roy's expertise
in this vital system. Roy has not let anything distract him in his
pursuit for perfection and if this aeroplane needs any trim inputs
to fly S&L, Roy will want to know the snagging pilot's name, who'll
then receive a visit from Roy to please explain himself. Roy, Paul
Wilkinson, and I are all 1961 apprentices and to work with them both
again after 45 years has been a particularly rare privilege. Roy we
were surprised to hear, has other interests in life, the Presidency
of a rifle club being the other draw on his time, and he departs tomorrow
to resume that alter ego. We gave Roy a send off tonight and will
miss his whirlwind way of working, where mini-tornadoes form shortly
after he has sprinted by. One of nature's real gentlemen, we will
feel your absence Roy, and are sorry you were not able to see your
baby fly before you left. In Sydney, my old mate, in Sydney." |
27
November 2006 |
Norman King,
QFM Flight Operations Administrator, reported from Southend: "We
have compiled a log of all the steps we have taken to determine
the reasons for #2 not starting. There were 18 by the time we had
finished at 1730. We have examined every external component connected
with fuel, air and ignition. For the record, we have performed:
1.
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Aural ignitor checks. |
2.
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Visual ignitor checks using an ignitor test box |
3.
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Interchange of plugs with known start ability |
4.
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Replacement of ignitor plugs with 7R4 types |
5.
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Increased
ignitor immersion depth
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6.
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External
substitution of a known ignitor box
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7.
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Removal and cleaning of Pressurising and Dump Valve Filter |
8.
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Replacement of Pressurising and Dump Valve |
9.
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Replacement of Micronic De-icing Filter |
10.
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Replacement of Fuel Pump |
11.
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Replacement of Fuel Control Unit |
12.
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Inputting a false burner pressure |
13.
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Comparison
of #1 and #2 burner pressures during spin
|
14.
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Check of 16th stage bleed leakage to turbocompressor |
15.
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Borescope of 16th stage ports through ignitor bosses. |
16.
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Check of Fuel Shutoff Valve and ignition sequencing |
17.
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Borescope of 16th stage area during wet spin |
18.
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Check of FCU drive from gearbox |
The number of
heads brainstorming this defect has been huge and in the final analysis,
the decision has been made to pull the engine. All agree that because
of what was discovered during step 15, with fuel wetting the fuel
manifold which is upstream of the burner cans, a manifold fracture
is indicated. Had a hangar been available for 24 hours, our friends
at Turbine Motor Works could have come to us, split the engine on-wing,
replaced the manifold all with a 24 hour turn time. Sadly, in this
heavy period of intense maintenance at Lasham's, no hangar is available.
Next best thing is that we have negotiated the use of Lasham's Engine
Shop into which our engine can go and TMW will send a team down
to do the job here at SEN. Transport time and costs are eliminated
and our down time is cut to a minimum. How many times have we said
that the support for our Project is beyond imagination? The cost
for all this? Parts only. Labour will be gratis. We shake our heads
in humility and the magic continues. Tomorrow #2 will be on a stand
and ready for strip. We shall overcome."
|
28
November 2006 |
|
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"Paul Wilkinson, one of our avionic engineers departed this morning
for home, with the aeroplane now so much the better in its electrical
state for Paul's unstinting effort over the five and a half weeks
this third time around Paul has given up to assist in the recovery
of XBA. We wished Paul bon voyage at dinner at the hotel last night.
We know Denis will miss him very much. Out to the airport again at
0740, bootstrap engine change specialists now, we had #2 on the Lasham's
Engine Shop floor by 1300. Two Turbine Motor Works engine specialists,
Mark Devine and Farai Tandi were waiting for us with almost all the
combustion chamber parts to rebuild ours should they find it necessary.
They soon had the 239 bolts out that connect each end of the case
and slid back the silver section of the engine to reveal the cans
and manifold. No trauma was found but a squirt up each half of the
removed manifold with compressed air resulted in a huge difference
in what was felt coming out of the spray nozzles, ranging from nil
to healthy. We compared this to the new manifold, which produced equal-feeling
jets of air from every nozzle. Significant. Mark and Farai estimated
a 2359 finish, so after clogging up their nozzles with the finest
Golden Arch gourmet fuel, we left them to it. We all were impressed
with their gracious nature and skill with their tools. These guys
have contributed in a major way to the Project, through the generosity
of their bosses Tom Vaughan and Dave Billington who deserve the thanks
of all of us who desperately want this aeroplane to come home. To
offset this great news, we had a setback today with an incident at
the hotel in which a robbery and arson attempt was made on the room
of one of our Team at around 1100 when we were all at work. He has
come through it with the upbeat spirit for which he is famous, with
the hotel proprietor promising to make good all the losses our great
mate has momentarily suffered. To respect his privacy, his identity
remains undisclosed. The hotel has one fewer room which it can sell
but we have one more experience that has enriched us and deepened
the Team spirit. The post-incident trauma counselling session, in
the form of a great Thai meal tonight with all those most concerned
helped end the day on a high note. We shall overcome." |
29
November 2006 |
|
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"Arrived at the Engine Shop at 0800 to see a note from the TMW
guys taped to the side of our #2 engine. Something to the tune of
Start You Bas....
At around 1530, it did. To the combined cheers of around 20 Lasham's
engineers including Ian Dorling, the QFM team and, in the distance,
all whose hopes for the aeroplane's good health had been in limbo
for a week, Peter lifted the start lever to end the run of 16 wet
starts. A cleaner start I have never seen, with instant light-off
and stable idle the reward we had all been hoping for, despite our
confidence in the trouble-shoot.
In other news, literally, Green Hornet was able to talk a newsagent
out of his Southend Echo Hotel Blaze banner and together with a copy
of the day's newspaper, presented them to our victim. To the credit
of the reporter, the story was quite accurate and factual. The flight
crew polished cowls, engine and turbocompressor inlets, Plucka assisting
with the engine installation.
We formally acknowledge the fantastic contribution made by Tom Vaughan,
Dave Billington, Mark Devine and Farai Tandi in giving us the perfect
fix and in record time. To Turbine Motor Works, we dips our lid.
With a lot of help, we have overcome" |
30
November 2006 |
|
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"I have great delight in handing today's report to Robert Phillips
and Bob Horn: The day we were all looking forward to - taxi tests;
but first the #2 engine micronic fuel filter to be replaced, P & D
filter to be removed, checked and replaced and hush kit and cowls
to be fitted. Aircraft ready for crew at 1200 with pushback at 1220.
Aircraft towed to runway for engine start. All team members were thoroughly
briefed by Roger Walter who was skipper for the taxi test and we proceeded
to our allotted tasks. All aspects of aircraft operations carried
out with periodic inspections by engineers in follow up vehicle. Power
runs and minor power and idle adjustments were made to # 2 Engine.
This was followed by a brief return to our tarmac spot for crew rotation
both ops and ground. 1st taxi test lasted 3 hours, 2nd taxi tests
were carried out at dusk, with logo and taxi lights blazing - showing
XBA in the best light. Engine accelerations and decelerations functional
tests performed. After the taxi tests were completed there were congratulations
all round. During after run checks, a "tinkling" noise was heard from
the #2 fan area which necessitated investigation. The N1 accessory
case and N1 tacho gear were removed with Bob Horn finding the offending
sheet metal clip in the drive shaft cavity. After rectification the
engine was restored to normal and engineers rejoined an anxious tech
crew at the hotel, where celebratory drinks were enjoyed by all. Due
to forecast bad weather, tomorrow has been declared a lay day. The
spotters had turned out in force to view/photograph the days activities."
|
01
December 2006 |
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"Layday declared due to weather. The troops welcomed a respite
from wrestling the weather, the aeroplane and each other." |
02
December 2006 |
|
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"At 0800 the engineering Team hit the hardstand, refreshed after
a layday, to check three P&D filters, pre-flight the aeroplane and
fuel her in preparation for her first test flight. The weather had
been threatening and there was some doubt in the early morning, with
rain falling and low cloud but we had an aim and thought positively.
The crew arrived at 1030, resplendent in full uniform and wearing,
not carrying, uniform caps - an example to their peers, and this was
sleepy Southend, not Seattle. They continued the standard that has
been applied to XBA from day dot.
Pre-flight complete, the photo op was taken and the last few moments
before departure were recorded, with all the QFM volunteers in frame
for the first time.
Doors closed and push back commenced as the usual loyal Lasham's supporters
gathered, seeming to have grown in number by a factor of two since
the taxi test.
Once again, Ridgeback was left seat, Feebs right, H at the panel,
Muz in the observer's and Plukka roving. In the cabin, Peter Elliott
and Denis Martin were tech observers and Ken Cannane completed the
complement.
The time had come.
Push back completed, the engine starts all routine, under the watchful
eyes of our great supporter, Tom Vaughan who had driven from Bury,
Cambridgeshire, to see us away. We were more than chuffed to have
him visit us. Once again, he made the offer of further assistance
should we have needed it, in between telling us of his own plans for
the future. They sound exciting.
So, the push back crew retreated to give hand signals on the right
and XBA was ready to taxi to the runway end while about 20 over-enthusiastic
photographers, QFM Team members, were chased back from the flight
strip by the ATC patrol saying they wouldn't let XBA depart until
we'd cleared the area.
Eight other aircraft were put into the hold while XBA lined up.
Lights on, take-off clearance was received.
The black smoke generators spooled up and the nose pitched up as the
brakes were released.
She was on her way.
A myriad cameras were focusing on the growing dart as gradually the
noise levels started to match the smoke levels and before we could
take it all in, through viewfinders, the wheels were off the ground
and VH-XBA was once again a flying machine.
All the effort of so many people had come to fruition. The joy overflowed
and I will remember forever the sight and sound once again of the
aeroplane I had cycled to Mascot to see arrive in 1959. The aeroplane
on which I gained my experience as an apprentice. So much of all the
Team's origins lay in this one 707.
Out of sight now, the smoke trail faded, we watched as she turned
to the north and disappeared.
Back to the hardstand, empty of our 707 for the first time in 6 years,
elated, relieved, excited, we headed for the Southend Terminal Coffee
Shop for a doorstop sandwich and for the first time, didn't need to
hurry back.
The test flight time was going to be around 3 hours and we took the
opportunity to put back so many of the stands we had been using over
the last few weeks, and tidied up the bay.
The time passed very quickly and a phone call from ATC told us that
XBA was 30 miles out.
Once again, a rush for the grass saw us searching the sky for our
baby.
The lights on this aero a giveaway and when the full set of fixed
and retractable landing lights are on, there's no mistaking the airframe
behind them.
We knew a missed approach was planned and the execution of this was
the highlight of the day.
The noise, the sight, the grace as she went around and into the red
sky at the end of a perfect day was poetic.
One more right circuit and the touchdown was featherlight, all reversers
doing their job.
XBA was back at Southend.
Right now, the entire Team is celebrating with QFM's blessing, with
the atmosphere unlike any felt here at the Erlsmere before.
We have had a life changing experience today, and achieved the unachievable." |
03
December 2006 |
|
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"A successful test flight is one thing, fixing the snags generated
by 2:23 flight time on an airframe that had had an extended holiday
is another.
Only six of us here to do the work of a dozen men means things take
longer, exacerbated by the ever-decreasing hours of daylight and colder
weather. We have to be careful on wet slippery stands and one of us
is sporting a really well scraped shin with a mis-step taken yesterday.
Early warning signs, perhaps?
The flight crew lent a hand today with screw removal on the elevator
balance bay access panels, in the troubleshooting of an elevator authority
snag following the test flight. This is one of the most tedious jobs
you can do on any aeroplane, removing the hundreds and hundreds of
screws that hold these 10 structural panels in place. OK if all the
screws are sound and have good slots for the #2 Phillips bit, but
in the case of XBA, not so lucky. Work will continue on this campaign
tomorrow.
The other defects found on TF1 are scheduled to be attacked tomorrow.
One obvious problem evident on taxi in yesterday were the two little
surfboard fins that had appeared in the dump chute area. Delaminated
skin in the dump chute fairing doors each side meant removal and presentation
to Lashams for re-skinning, work well progressed at close of business
today. We also have to chase a nose gear hydraulic leak, a task to
start tomorrow with an upline leak check. This means selecting the
gear lever UP with hydraulic power on the aircraft. Despite gear pins
in place and the nose gear double locked with two separate pins, it's
still a procedure that goes against the thinking engineer's principles,
and is always completed with a profound sense of relief.
Green Hornet, displaying her Good Housekeeping Diploma in Tidiness
and Cleanliness went over the entire cabin today, vacuuming, polishing,
scrubbing, disinfecting, polishing, sweeping, deodorising, waxing,
polishing and did I mention polishing? The place is almost too good
to occupy and woe betide the first person to leave a finger mark on
her diamond-sparkling cabin windows. We may have to wear white overalls
before we can sit down in the crew rest, let alone venture into the
main areas. Jokes aside, the difference this has made to the ambiance
is truly wondrous to see, and the passengers will be sure that they
will be in the neatest aeroplane cabin they will ever again likely
to be.
Two Qantas 747-400 pilots dropped in today on their LHR slips. We
said hello to Dick Hodder, a QFM Committee Member, in the finance
area, and Sandy Howard, well-known Super Connie pilot. More hard slog
tomorrow." |
04
December 2006 |
|
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"Those 300-odd screws that hold on the balance bay access panels
on the right elevator did what they were supposed to do and held on
- with a few dozen not wanting to let go without their heads being
drilled off. When eventually they did release we found nothing untoward,
no birds nests, nothing loose, nothing jammed. So, with a clean up
and a light lube, the break-away force at the trailing edge was within
the limits and normal.
In another fix, the nose gear hydraulic leak was detected on the upline
check. With a nose jack in place as belt and two braces, the weep
was clearly evident when the gear lever was placed UP and with about
a third of a turn on a B nut, the loss of fluid should now be cured.
Again, Bob Horn had another win under his belt.
The goodness continued when Denis Martin went looking in the Lasham's
loft, the repository for 707 bits from a time past. We had a Radio
Altimeter problem and a Transmitter/Receiver was the suspect. No surprise,
there was one on the shelf, serviceable and ready to go, and go it
did, problem fixed.
The two dump chute fairing doors were presented to us by Jonathon
Spicer, freshly skinned, chromated inside and Boeing Gray outside,
and with their installation, another area about which there will be
no concern.
We are beginning to feel the aeroplane is submitting, albeit slowly,
to our ministrations, and had we more arms and legs, it would have
been ready for flight again tomorrow. The installation of the balance
panels will be a 3-4 hour job tomorrow if all the framies get stuck
into it. Together with the avionic work still outstanding, the radar
indicator still out for work, for example, there will be too much
for 6 people to handle as well as pre-flighting and fuelling XBA for
another test flight. So, no flying tomorrow." |
05
December 2006 |
|
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"The task for the day? Replace the 700-odd screws in the elevator
balance panels and button them up again, for the last time, we hope.
Denis Martin chased a radio snag that developed overnight and installed
the radar indicator. We had it all cleaned up by lunch time and celebrated
with Tesco Caesar Salad in the plush surrounds of the Stateroom onboard
the 707. A few of us had an eyelid inner surface inspection for a
few moments and felt relaxed with the state of the aeroplane, once
again, a great feeling, I tell you. The two Flight Engineers (yes
folks, there are Flight Engineers on this aeroplane, something the
publicity machine seems not have noticed) fuelled the aero and put
on around 23 000 litres of gas, on Muz's credit card to the tune of
GBP5500, which according to H works out at 46.52 pence/l, plus 17.5%
VAT. The pilots once again worked a new route home with the weather
in the eastern US driving us further south, just like all migrating
birds, to warmer climes. Montreal and Seattle now give way to Orlando
and Long Beach. Weather tomorrow looks suitable for flying, and Test
Flight 2 is scheduled to depart at 0830, with a return at 1200-ish.
For this next operation we are down to 5 engineers with the loss of
our marvellous mate and colleague Bob Horn, who returns to SYD tomorrow
morning on the 32 at 1115. This means he will be sharing breakfast
with us at 0600 and we will all depart together, he for home and we
for another day at SEN. We will be short one absolutely inspiring
man, whose work rate is second to none. He has taught me much about
the aeroplane and as he said at the farewell dinner at the Esplanade,
we have learnt all about this aeroplane short of figuring out the
potable water system. It will be a different scene here without him.
He did at least have the pleasure of seeing XBA fly, which naturally,
was the highlight of his time here. We saw Muz after Peter and I returned
from Air Livery's graphics department where we collected the sponsors
and supporters decals which will adorn the fuselage at the Door Left
1 position. Muz commented that it was good to see the aeroplane with
no stands underneath it and with all the engine blanks in place. A
feeling of completion is creeping over us. Let's hope the reality
reflects this. At 1230 tomorrow, will know." |
06
December 2006 |
|
Robert
Dr Bob Phillips reported from Southend: "The second
Test Flight for XBA was scheduled for 0830 this morning. All preparations
proceeded as normal with all the crew again in full uniform and the
Green Hornet (Karen Glass) fully equipped with 5 cameras, scarf and
cold weather jacket. Ken Cannane, Norm MacKay and Robert Phillips
were honoured and privileged to be the engineering observers for the
Test Flight. Items on the agenda for today's flight were testing of
the elevator control system after rectification, electric flap operation,
outboard speed brake operation, and emergency gear extension with
performance data and fuel flows to be ascertained and finally cabin
altitude warning functional check . With everyone on board push back
was at 0900, taxi commenced at 0915, take-off 0925. What a ripper!
This little baby is a sky rocket. Today's operation was between Norwich,
Cambridge and Peterborough with ATC direction mainly from RAF Wattisham.
Crew reported an improvement in the longitudinal control, which meant
the elevator balance panel work over the last two days had made a
difference. The fuel dump system was also checked and some of the
precious stuff was sacrificed for the occasion. The two FEOs, H and
Plucka, exercised the cabin temp control through its full range and
in the warmth of the cabin, some people had a short zizz. Provisions
thoughtfully provided by Karen enabled the observers to experience
tea and bikkies in the stateroom. At the completion of the test flight,
RAF Wattisham requested we carry out an ILS check, an obligation fulfilled
accurately and with the appropriate minimas observed. The time was
now 1145. Following this last detail, we tracked to SEN for another
missed approach at 1207, went around for a landing at 1219. Total
flying time was 2.9 hours. Meanwhile back at the hut, Karen went on
a Tesco and Aldi expedition to purchase the dry goods for the flight.
Post flight de-briefing was carried out and the defects revealed just
enough work to fill a day tomorrow. Out of this was the momentous
decision that departure date will be Friday, 8 December at 0830. Can
you believe it, we are going home!" |
07
December 2006 |
|
Norman
King, QFM Flight Operations Administrator, reported from Southend:
"The Last Epistle From SEN. Here endeth a chapter, but also beginneth
a journey. If you have ever packed for a long road trip, and you thought
the boot was too small, let me assure you even the two boots in the
707 are only just big enough for what we have to take home. The tooling,
flight spares, oils, fluids, baggage, et al will occupy most of the
space. Packing it took most of the day and Plucka and H put in a huge
effort and loaded the aeroplane with their close eye on the C of G,
hoicking about 1.2 tons of gear into the two holds. In the process,
we had two tornadoes go through the airport, one of them blowing stands
and equipment around and even our several hundred kilo front steps
took off and headed for #2 at an increasing rate of knots as I watched
helplessly from Door Left 1. Miraculously, Peter raced in from the
nose and tackled the fast charging steel monster, slowing it just
enough to prevent it from causing any damage despite a kiss against
the nose cowl lip, protected by the yellow engine blank. The weather
seemed to be making a point. Sleet added to the statement. The farewells
were said today, with Ian Dorling hosting a personal farewell to us
all in the Boardroom during which we presented him with the two flags
which had flown above our hut every day since the project commenced,
framed and inscribed. We paid our respects to the dozens of friends
we have made and took their good wishes with us. In all Projects,
the operational aspects all pretty much follow the same path. Identify
the task, allocate the manpower, buy the parts, repair the parts,
fit the parts, test. What has made these thousands of individual jobs
flow has been the indescribable kindred spirit we have with all the
Lashams guys. They, under Ian Dorling's avuncular leadership style,
reflect his view of life. Treat others as you would wish to be treated
yourself. The Golden Rule has made this Project work in a way that
I had never experienced before. ATC Lasham Ltd - Thank you from your
greatest admirers, the QFM Preservation Project Engineers and Flight
Crew. The next report will be from the first port from which I can
dispatch a post. Tenerife, perhaps. Our good mates, Robert Phillips
and Norm MacKay will see us off tomorrow and close up the station.
We will miss their positive, upbeat company and look forward to our
reunion in SYD on Saturday, 16 December 2006." |
The
QFM 707 Project |
Daily
Diary
|
Slideshow
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30JAN06
to 21NOV06 |
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22NOV06
to 07DEC06 |
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08DEC06
to 27JUL07 |
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